Improvement of Motor Control System in J-PARC Linac and RCS

Autor: Takahashi, Hiroki, Kawase, Masato, Miura, Akihiko, Sawabe, Yuki, Suzuki, Takahiro, Yoshimoto, Masahiro
Jazyk: angličtina
Rok vydání: 2018
Předmět:
DOI: 10.18429/jacow-ipac2018-wepal015
Popis: In J-PARC, at the Linac wire scanner, the RCS collimator, and etc., a motor control system by VME is constructed as a drive system of them. Since the malfunction of operation occurred in the control system of the RCS collimator drive system in 2016, we decided to improve the motor control system. As a cause of malfunction, it is considered that aging of control equipment is one of them as J-PARC has been operated for more than 10 years. However, the defect did not occur in the reproduction test. Therefore, it can be considered that a malfunction occurred in the VME control system due to abnormality of the semiconductor element due to radiation ray. Then, in the improved motor control system, PLC with FA* specification with high reliability was adopted as the control device. Also, in case of unexpected event that a malfunction occurred in the PLC, the emergency stop mechanism was developed to stop the drive system by the signal of the limit switch, and a system incorporating it was constructed. In this paper, we show the inference of cause of the malfunction and details the improved motor control system with high safety.
Proceedings of the 9th Int. Particle Accelerator Conf., IPAC2018, Vancouver, BC, Canada
Databáze: OpenAIRE