Multistage Tool Path Optimisation of Single-Point Incremental Forming Process
Autor: | Khamis Essa, Naser A. Alsaleh, Hany Hassanin, Jrp Djuansjah, Mahmoud Ahmed El-Sayed, Mahmoud Ahmadein, Zhou Yan, Hossam Mohamed Eldessouky |
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Jazyk: | angličtina |
Rok vydání: | 2021 |
Předmět: |
Technology
business.product_category Computer science optimisation forming Base (geometry) Mechanical engineering Article incremental Range (statistics) General Materials Science FEA sheet metal Microscopy QC120-168.85 Design of experiments QH201-278.5 Process (computing) Forming processes tool path Engineering (General). Civil engineering (General) Finite element method TK1-9971 SPIF Descriptive and experimental mechanics visual_art visual_art.visual_art_medium Die (manufacturing) Electrical engineering. Electronics. Nuclear engineering TA1-2040 Sheet metal business |
Zdroj: | Materials, Vol 14, Iss 6794, p 6794 (2021) Materials Materials; Volume 14; Issue 22; Pages: 6794 |
ISSN: | 1996-1944 |
Popis: | Single-point incremental forming (SPIF) is a flexible technology that can form a wide range of sheet metal products without the need for using punch and die sets. As a relatively cheap and die-less process, this technology is preferable for small and medium customised production. However, the SPIF technology has drawbacks, such as the geometrical inaccuracy and the thickness uniformity of the shaped part. This research aims to optimise the formed part geometric accuracy and reduce the processing time of a two-stage forming strategy of SPIF. Finite element analysis (FEA) was initially used and validated using experimental literature data. Furthermore, the design of experiments (DoE) statistical approach was used to optimise the proposed two-stage SPIF technique. The mass scaling technique was applied during the finite element analysis to minimise the computational time. The results showed that the step size during forming stage two significantly affected the geometrical accuracy of the part, whereas the forming depth during stage one was insignificant to the part quality. It was also revealed that the geometrical improvement had taken place along the base and the wall regions. However, the areas near the clamp system showed minor improvements. The optimised two-stage strategy successfully decreased both the geometrical inaccuracy and processing time. After optimisation, the average values of the geometrical deviation and forming time were reduced by 25% and 55.56%, respectively. |
Databáze: | OpenAIRE |
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