Zobrazeno 1 - 10
of 26
pro vyhledávání: '"S. L. N. Desikan"'
Publikováno v:
Acta Astronautica. 185:78-88
Experiments were carried out to assess the effect of rear face geometrical modifications of a wall mounted rectangular cavity on pressure fluctuations at supersonic speed. Initially, tests were conducted on a base cavity of length to depth ratio of 3
Publikováno v:
AIAA Journal. 58:1206-1215
Time-resolved schlieren images and unsteady pressure measurements were employed to understand the flowfield characteristics of a rectangular cavity at Mach number 1.8 with a unit Reynolds number of...
Publikováno v:
AIAA Journal. 57:3773-3778
Experiments were carried out on a rectangular cavity (L/D=4) to study the effects of interaction between a transient shock system and a cavity shear layer on cavity oscillations through high-speed ...
Publikováno v:
Proceedings of the National Aerospace Propulsion Conference ISBN: 9789811550386
Experiments were performed to study the effect of cavity rear wall modification at different L/D ratios of an open cavity. All the experiments were carried out at Mach 2.0 and corresponding Reynold’s number of 5.5 × 105 based on cavity depth. Unst
Externí odkaz:
https://explore.openaire.eu/search/publication?articleId=doi_________::4eb02b07d63261e66520f6c2806d6978
https://doi.org/10.1007/978-981-15-5039-3_24
https://doi.org/10.1007/978-981-15-5039-3_24
Publikováno v:
Journal of Fluids Engineering. 142
Experiments are carried out in supersonic flow past cavities (L/D = 1–3) to comprehend cavity oscillation from transverse to longitudinal mode. To characterize this, time-resolved schlieren images and unsteady pressure measurements are carried out.
Publikováno v:
AIAA Journal. 56:3600-3609
Experiments were carried out on a scaled model of scramjet engine with gaseous hydrogen as a fuel in a 1 m combustion-driven shock tunnel. The simulated enthalpy was 2.6 MJ/kg, at a freestream Mac...
Autor:
K. Srinivasan, S. L. N. Desikan
Publikováno v:
Journal of Spacecraft and Rockets. 55:1144-1153
Experiments were carried out to bring out the effects of the single vertical tail (SVT) and the twin vertical tail (TVT) of a typical winged reentry vehicle on aerodynamic coefficients at supersoni...
Publikováno v:
Experimental Thermal and Fluid Science. 80:348-362
Experiments were carried out on a blunt-cone-cylinder geometry with various flared aft body configurations to understand the effect freestream (M = 5)-jet plume (M = 2.65) interaction on aerodynamic coefficients. Supersonic jet plume of varying press
Publikováno v:
Aerospace Science and Technology. 113:106688
Hypersonic intake with 20 and 30% blockage struts is experimentally investigated in Mach 6 flow. Initially the experiments are conducted with full opening of the cowl at fixed condition. The results show that the intake is started for 20% blockage st
Publikováno v:
Current Science. 120:81
As a prologue to the Gaganyaan project, ISRO successfully test fired one of the critical and essential technologies for human space flight, i.e. Crew Escape System (CES) Pad Abort Test on 5 July 2018. This is a strategically important flight as a par