Zobrazeno 1 - 10
of 27
pro vyhledávání: '"Paul F. Beard"'
Publikováno v:
International Journal of Turbomachinery, Propulsion and Power, Vol 6, Iss 3, p 29 (2021)
An investigation of hot gas ingestion driven by the disc pumping effect in a chute seal was conducted at the Oxford Rotor Facility. Measurements of mean pressure, unsteady pressure and gas concentration have been logged and analysed under different o
Externí odkaz:
https://doaj.org/article/7c93d6f268814dcc892e95d7a58ea734
It is known that a secondary effect of rotor-casing effusion cooling is to modify and potentially spoil the rotor over-tip leakage flow. Studies have shown both positive and negative impacts on high-pressure (HP) stage aerodynamic performance and hea
Externí odkaz:
https://explore.openaire.eu/search/publication?articleId=doi_dedup___::f0ed07046aee39967e8c3cdc092b2f16
https://doi.org/10.1115/1.4050019
https://doi.org/10.1115/1.4050019
This paper presents wall-modeled large-eddy simulations (WMLES) of a chute-type turbine rim seal. Configurations with an axisymmetric annulus flow and with nozzle guide vanes fitted (but without rotor blades) are considered. The passive scalar concen
Externí odkaz:
https://explore.openaire.eu/search/publication?articleId=doi_dedup___::867a619fe6a838a75d2842f13e2e206d
https://doi.org/10.1115/1.4049487
https://doi.org/10.1115/1.4049487
Publikováno v:
Volume 10B: Turbomachinery — Axial Flow Turbine Aerodynamics; Deposition, Erosion, Fouling, and Icing; Radial Turbomachinery Aerodynamics.
Over the last years, advanced experiments under engine-representative conditions have been performed in the Oxford Turbine Research Facility (OTRF) to obtain high-quality aero-thermal data that are essential for developing novel cooling designs and f
Publikováno v:
Volume 6B: Heat Transfer — General Interest/Additive Manufacturing Impacts on Heat Transfer; Internal Air Systems; Internal Cooling.
A chute rim seal cavity has been instrumented with time-resolved and time-averaged pressure transducers as well as a gas concentration measurement system at the Oxford Rotor Facility. The unsteady pressure transducers were unevenly distributed along
Publikováno v:
AIAA Propulsion and Energy 2021 Forum.
This experimental study considered the performance of a chute rim seal downstream of turbine inlet guide vanes (but without rotor blades). The experimental set up reproduced rotationally-driven ingestion without vanes and conditions of pressure-drive
Externí odkaz:
https://explore.openaire.eu/search/publication?articleId=doi_dedup___::f07742ac63e348a44434eb1261a4b4b7
https://doi.org/10.1115/1.0002993v
https://doi.org/10.1115/1.0002993v
Autor:
Paul F. Beard, Chiara Falsetti, Robert Camilleri, Cinzia Giacomuzzo, Alessandro Francesconi, Lorenzo Olivieri, Leonardo Barilaro
Publikováno v:
2021 IEEE 8th International Workshop on Metrology for AeroSpace (MetroAeroSpace).
The ever-increasing number of earth-orbiting spacecraft and related space junk is resulting in a dramatic rise in the risk of space debris impacting and damaging satellites and thereby negatively affecting the regular execution of several services pr
Publikováno v:
Journal of Turbomachinery. 143
Recently developed lean-burn combustors offer reduced NOx emissions for gas turbines. The flow at exit of lean-burn combustors is dominated by hot streaks and residual swirl, which have been shown—individually—to impact turbine aerodynamic perfor
Publikováno v:
European Conference on Turbomachinery Fluid Dynamics and Thermodynamics.
This paper presents the calibration method and error evaluation for an infrared (IR) measurement system implemented on the upgraded Oxford Turbine Research Facility (OTRF). The OTRF is a world leading turbine test facility capable of matching engine