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pro vyhledávání: '"Jin Tso"'
Autor:
Jin Tso, Daniel Biezad
Publikováno v:
2001 Annual Conference Proceedings.
Publikováno v:
International Journal of Aeroacoustics. 5:173-191
An experiment was conducted to investigate the flow-induced nose-cone cavity oscillations of a B&K in-flow microphone. A 38.1-mm-diameter scale model of the B&K 12.7-mm UA 0386 nose cone was constructed and tested in a 177.8-mm-round free-jet in the
Publikováno v:
Journal of Aircraft. 41:1404-1413
An experiment was performed in a water tunnel on a Boeing-Vertol VR-7 airfoil to study the effects of tangential blowing over the upper surface. Blowing was applied at the quarter-chord location during sinusoidal pitching oscillations described by al
Autor:
Mark D. Buchholz, Jin Tso
Publikováno v:
Journal of Aircraft. 37:1050-1057
A wind-tunnel experiment was conducted on a 60-deg delta wing at low speeds and low angles of attack to determine the lift augmentation effects of the leading-edge fences and a Gurney flap. Lift, drag, pitching moment, and surface pressures were meas
Publikováno v:
40th Fluid Dynamics Conference and Exhibit.
8. Through the contribution of these authors the development and lifetime of the fully developed wing-tip vortex is relatively well understood. Many of these experimental methods have had difficulties resolving the vortex core. These difficulties ste
Publikováno v:
24th AIAA Applied Aerodynamics Conference.
An active ∞ow control experiment was conducted on a 2-ft chord NACA 0036 airfoil in a 3-ft by 4-ft Wind Tunnel at Re = 1:0 £ 10 6 . The model was equipped with oscillatory jet actuators at x/c = 0.30 and 0.65 that provided 120 Hz periodic excitati
Autor:
James E. Knight, Jin Tso
Publikováno v:
23rd AIAA Applied Aerodynamics Conference.
An experiment was conducted to compare the base-drag reduction of a bluff body employing various passive control means. A 1-ft-long bluff-body model with a blunt square base was tested in the Cal Poly 3’ x 4’ ft lowspeed wind tunnel at three fore
Autor:
Jin Tso, Michael Keidel
Publikováno v:
35th Joint Propulsion Conference and Exhibit.
Publikováno v:
16th AIAA Applied Aerodynamics Conference.
The Boeing-Vertol VR-7 airfoil was experimentally studied with steady and pulsed upper-surface blowing for sinusoidal pitching oscillations described by alpha = alpha(sub m) + 10 deg sin(omega t). The tests were conducted in the U.S. Army Aeroflightd
Publikováno v:
3rd AIAA/CEAS Aeroacoustics Conference.
One source contributing to wind tunnel background noise is microphone self-noise. An experiment was conducted to investigate the flow-induced acoustic oscillations of Bruel & Kjaer (B&K) in-flow microphones. The results strongly suggest the B&K micro